The problem became evident after 17 days in service and the engine was taken out of service immediately. The rear wheels have been dropped out and despatched to Ian Riley Engineering at Bury where the problem will be rectified. Whilst initially it was feared the down time in obtaining a new axle and fitting it, with the attendant problems of specifying and obtaining the correct grade of steel, would be considerable, it is likely that an engineering solution can be achieved that will permit the existing axle to be reused.
The down time is likely, therefore, to be around two months, after which our highly popular 'new' 2-8-0 can get back to work. Updates on progress will be issued from time to time.
© South Devon Railway Trust 2006